ENABLE MIDSTREAM PARTNERS, LP

hazardous_liquid Incident — — October 14, 2018

Incident Information

Incident DateOctober 14, 2018
OperatorENABLE MIDSTREAM PARTNERS, LP
CommodityHVL OR OTHER FLAMMABLE OR TOXIC FLUID WHICH IS A GAS AT AMBI
Pipeline Typehazardous_liquid

Location

State
Coordinates32.42684, -94.56173

Cause

CauseCORROSION FAILURE
SubcauseEXTERNAL CORROSION

Casualties

Fatalities0
Injuries0

Costs

Property Damage$48,200
Emergency Response$5,000
Other Costs$0

Location Map

Incident Narrative

ON 10-14-18 A LEAK WAS FOUND BY A LAND OWNER IN HARRISON COUNTY, TEXAS. THE LANDOWNER IMMEDIATELY NOTIFIED ENABLE GAS TRANSMISSION SYSTEM CONTROL. AN O&M TECHNICIAN WAS DISPATCHED TO VERIFY IF THE LEAK AND IT WAS CONFIRMED THAT LINE AJ-3 WAS LEAKING. THE RESPONDING EMPLOYEES THEN CONTACTED GAS CONTROL AND THE HARRISON CO SHERIFF'S OFFICE. THE LINE WAS TAKEN OUT OF SERVICE AND A REPAIR WAS MADE. DURING THE RELEASE, THE LIQUID ETHANE IMMEDIATELY VAPORIZED WHEN EXPOSED TO AIR RESULTING IN A LARGE ICE CRATER AT THE LEAK SITE. FIELD EXAMINATION OF THE LINE SHOWED LOCALIZED PITTING WITH A PINHOLE IN THE PIPELINE. THE DEFECT WAS REMOVED AND SENT FOR ANALYSIS. THE RESULTS OF THE ANALYSIS HAVE NOT BEEN COMPLETED AND A SUPPLEMENTAL REPORT WILL BE SUBMITTED WHEN THE ANALYSIS IS RECEIVED. THE INCIDENT WAS REPORTED TO THE NRC ON 10/14/2018 AT 19:29 CST (NRC #1227477) AND THE 48 HOUR FOLLOW UP (1227588) WAS PROVIDED ON 10/16/2018 09:15. ENABLE RECEIVED THE METALLURGICAL REPORT FROM THE LAB. THE LAB CONFIRMED THE CAUSE OF THE PINHOLE WAS STRAY CURRENT CORROSION, BUT COULD NOT IDENTIFY SPECIFICALLY AC OR DC. ENABLE FIELD INVESTIGATIONS AND MEASUREMENTS LEAD US TO BELIEVE THAT IT WAS STRAY AC CURRENT. SUPPLEMENTAL 3/20/2019 PART H NARRATIVE

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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