PHILLIPS 66 PIPELINE LLC
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | PHILLIPS 66 PIPELINE LLC |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 35.94710, -96.75301 |
Cause
| Cause | CORROSION FAILURE |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
THIRD PARTY OPERATOR NOTIFIED CUSHING/BUXTON FACILITY OF CRUDE DISCOVERED ON THE SURFACE OF THE GROUND BETWEEN CUSHING AND BUXTON STATIONS. PIPELINE OPERATIONS EXCAVATED AND DISCOVERED A PIN HOLE LEAK ON THE BEND OF THE 12INCH INNER TRANSFER LINE FROM THE LACT UNITS TO THE CUSHING STATION TANKS. SEGMENT WAS REMOVED AND SENT TO LAB FOR METALLURGICAL ANALYSIS. LINE WAS REPAIRED AND PLACED BACK INTO SERVICE ON 10/31/2018 2019-1-8 - UPDATED PART G, ITEM 8. RESULTS DETERMINED BASED ON METALLURGICAL ANALYSIS.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.