SFPP, LP

hazardous_liquid Incident —

Incident Information

Report Date
OperatorSFPP, LP
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates38.75560, -121.27675

Cause

CauseEXCAVATION DAMAGE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

AT 11:20 A.M. ON 11/2/2018, A 3RD PARTY CONTRACTOR CALLED THE ROCKLIN CONTROL ROOM REPORTING THEY HAD JUST STRUCK A PIPELINE WITH AN AUGER WHILE CONDUCTING GEOTECHNICAL SURVEYS ALONG THE RAILROAD RIGHT OF WAY. IT WAS DETERMINED THAT LS-48 HAD BEEN STRUCK AND DIESEL WAS RELEASED FROM THE LINE AS THE STATIC PRESSURE IN THE LINE DROPPED FROM 70 PSI TO 0. THE LINE WAS EXCAVATED, PURGED, AND THE DAMAGED PORTION CUT OUT AND REPLACED WITH A NEW PIECE. AFTER SUCCESSFUL STATIC AND RUNNING TESTS, THE LINE WAS RETURNED TO NORMAL SERVICE AND REMEDIATION ACTIVITIES CONTINUED FOR SEVERAL WEEKS AFTERWARD UNTIL THE MAJORITY OF THE CONTAMINATED SOIL HAD BEEN REMOVED TO THE EXTENT PRACTICABLE. AN INVESTIGATION INTO THE ACCIDENT REVEALED THAT LS-48 DID NOT HAVE PROPER MARKINGS AT THE TIME OF THE INITIAL LOCATE OR AT THE TIME OF THE INCIDENT, HOWEVER, THE PARALLEL SFPP LS-20 WAS PROPERLY MARKED. 1/30/2019 UPDATE- NO EDITS OR ADDITIONS FROM ORIGINAL. FINAL SUPPLEMENTAL SUBMITTED.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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