"MAGELLAN PIPELINE COMPANY, LP"
hazardous_liquid Incident — — June 8, 2020
Incident Information
| Incident Date | June 8, 2020 |
| Operator | "MAGELLAN PIPELINE COMPANY, LP" |
| Commodity | REFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 36.14799, -96.03286 |
Cause
| Cause | EXCAVATION DAMAGE |
| Subcause | EXCAVATION DAMAGE BY OPERATOR'S CONTRACTOR (SECOND PARTY) |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | $2,333,500 |
| Emergency Response | $585,000 |
| Other Costs | $0 |
Location Map
Incident Narrative
"AT 14:28 ON JUNE 8, 2020, MAGELLAN'S TULSA - BARNSDALL #4-12"" PIPELINE WAS IMPACTED BY A SECOND PARTY LINE STRIKE DURING HORIZONTAL DIRECTIONAL DRILLING OPERATION. AT THE TIME OF THE INCIDENT, MAGELLAN'S CONTRACTOR WAS PERFORMING THE PILOT HOLE OPERATION FOR THE #3-12"" PIPELINE REPLACEMENT ACROSS THE ARKANSAS RIVER AND STRUCK THE #4-12"" PIPELINE NORTH OF THE ARKANSAS RIVER BETWEEN THE NORTH LEVEE AND CHARLES PAGE BLVD. CODE RED RESPONSE WAS INITIATED AND FIELD PERSONNEL WERE DISPATCHED TO FURTHER ISOLATE THE BLOCKED IN SECTION WITH MANUAL VALVES AND BEGIN CLEANUP ACTIVITIES. AT THE TIME OF THE INCIDENT, THE PIPELINE WAS SHUT DOWN AND ISOLATED WITH REMOTE ISOLATION VALVES. THE #4-12"" PIPELINE WAS RETURNED TO SERVICE BY COMMISSIONING A NEWLY INSTALLED HDD REPLACEMENT CROSSING FOR THE #1-12"". THE IMPACTED PIPELINE SEGMENT WILL BE GROUT FILLED AND ABANDONED IN PLACE. THE PUNCTURE SIZE IS AN ESTIMATE BASED ON RELEASE VOLUME. NRC 48-HOUR UPDATE: #1279210, 06/09/14:12 SUPPLEMENTAL/FINAL:(09/11/2020) PART A11, D8, E9, G3-17, H"
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.