COLONIAL PIPELINE CO

hazardous_liquid Incident — — July 7, 2020

Incident Information

Incident DateJuly 7, 2020
OperatorCOLONIAL PIPELINE CO
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates30.71093, -91.28376

Cause

CauseEQUIPMENT FAILURE
SubcauseTHREADED CONNECTION/COUPLING FAILURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$5,000
Emergency Response$5,000
Other Costs$0

Location Map

Incident Narrative

"ON TUESDAY, JULY 7, 2020, AT APPROXIMATELY 10:00 AM CST, WHILE CONDUCTING A WALKTHROUGH CHECK OF MANIFOLD #2, OPERATIONS PERSONNEL OBSERVED AN OPEN EXCAVATION FILLED WITH DISCOLORED WATER AND HAVING A PETROLEUM ODOR. THE DISCOLORED WATER WAS TESTED AND FOUND TO BE POSITIVE FOR PRODUCT (DIESEL). LOCAL PROJECT MANAGERS, INSPECTORS AND THE ENVIRONMENTAL SPECIALIST RESPONDED TO THE SCENE. AT APPROXIMATELY 10:15 AM CST A VAC-TRUCK BEGAN REMOVING FREESTANDING PRODUCT AND WATER OUT OF THE EXCAVATION. AT APPROXIMATELY 14:40 PM CST, THE EXCAVATION WAS CLEARED AND THE SOURCE OF THE RELEASE WAS IDENTIFIED AS A LOOSE TOR CONNECTION ON THE 151 TANK LINE. AT 15:04 PM CST, THE TOR WAS TIGHTENED AND STOPPED THE RELEASE SOURCE. THIS AREA HAD BEEN EXCAVATED ON JUNE 29, 2020, TO ACCOMMODATE TAKING THE TANK OUT OF SERVICE (OOS) FOR SCHEDULED 653 MAINTENANCE WORK. ALL RELEASED PRODUCT WAS CONTAINED ON CPC PROPERTY AND DID NOT RESULT IN AN EMERGENCY CONDITION. THE RELEASE VOLUME WAS 16 GALLONS AND ALL REMEDIATION ACTIVITIES HAVE BEEN COMPLETED. BASED ON THE RELEASED VOLUME AND COST OF REPAIRS/RESPONSE, NO EXTERNAL EMERGENCY NOTIFICATIONS WERE WARRANTED."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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