DCP MIDSTREAM

hazardous_liquid Incident — — July 16, 2020

Incident Information

Incident DateJuly 16, 2020
OperatorDCP MIDSTREAM
CommodityHVL OR OTHER FLAMMABLE OR TOXIC FLUID WHICH IS A GAS AT AMBI
Pipeline Typehazardous_liquid

Location

State
Coordinates29.06306, -95.75596

Cause

CauseEQUIPMENT FAILURE
SubcauseMALFUNCTION OF CONTROL/RELIEF EQUIPMENT

Casualties

Fatalities0
Injuries0

Costs

Property Damage$18,000
Emergency Response$0
Other Costs$0

Location Map

Incident Narrative

"ON 07/16/2020, AT 7:41 AM, DCP FIELD TECHNICIAN IDENTIFIED A LEAK IN A VALVE BODY BYPASS NIPPLE OF SWEENY METER STATION. AFTER THE CONFIRMED DISCOVERY OF THE LEAK, A PLAN WAS PUT INTO PLACE TO LAUNCH A 24 INCH PIG TO DISPLACE THE NGL BACK INTO THE SAHI MAINLINE. ONCE THE PIG WAS LAUNCHED AT 1:33 AM, 07/17/2020, IT ISOLATED THE LEAK DUE TO N2 BEING BEHIND THE PIG. IT WAS DETERMINED THAT THE PROVIDED VALVE FROM THE MANUFACTURER HAD A DEFECTIVE THREADED NIPPLE WHICH CAUSED LEAK. AS A CORRECTIVE ACTION, DCP WAS PROVIDED A NEW VALVE FROM THE MANUFACTURER AND WAS INSTALLED AT THE METER STATION."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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