TEXOMA CRUDE OIL PIPELINE CO., LLC
hazardous_liquid Incident — — March 11, 2019
Incident Information
| Incident Date | March 11, 2019 |
| Operator | TEXOMA CRUDE OIL PIPELINE CO., LLC |
| Commodity | CRUDE OIL |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 34.20242, -97.48605 |
Cause
| Cause | CORROSION FAILURE |
| Subcause | INTERNAL CORROSION |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | $5,000 |
| Emergency Response | $52,000 |
| Other Costs | $0 |
Location Map
Incident Narrative
FINAL SUPPLEMENTAL REPORT SUBMITTED 08-05-2019, DUE TO CLEAN-UP COMPLETE. COPY OF CORRECTIVE ACTION REPORT (CAR) SENT TO U.S. EPA AND OCC. UPDATED FINAL ANTICIPATED COSTS IN PART D. NO OTHER CHANGES MADE ON THIS REPORT. CONTRACT CARRIER (TRUCK DRIVER) NOTICED OIL ON THE GROUND AND CALLED TCOP EMERGENCY NUMBER. SYSTEM WAS SHUT DOWN. TCOP OPERATIONS PERSONNEL WENT ON SITE TO DISCOVER IMPACTED SOIL AND CREEK. EMERGENCY RESPONSE PROCEDURES WERE ACTIVATED AND ADDITIONAL PERSONNEL WERE NOTIFIED AND DISPATCHED TO SITE. AFTER RELEASE AREA WAS CLEARED OF HAZARDS, EXCAVATION OF THE AREA REVEALED THE AFFECTED PIPE. A PLEDCO CLAMP WAS APPLIED AND SYSTEM WAS PLACED BACK IN SERVICE. NOTE THIS LINE IS A DUAL 3"" AND 4"" SIZE LINE. UPDATED REPORT SUBMITTED TO NRC (REPORT #1242825) ON 04-15-2019. NO CHANGES IN VOLUME, JUST STATUS UPDATE. INVESTIGATION DETERMINED INTERNAL CORROSION CAUSED THE PIPE TO DEVELOP A HOLE WHICH RESULTED IN THE RELEASE.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.