CHEVRON PIPE LINE CO
hazardous_liquid Incident — — April 19, 2019
Incident Information
| Incident Date | April 19, 2019 |
| Operator | CHEVRON PIPE LINE CO |
| Commodity | REFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 38.02178, -122.06197 |
Cause
| Cause | EQUIPMENT FAILURE |
| Subcause | MALFUNCTION OF CONTROL/RELIEF EQUIPMENT |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | $1,500 |
| Emergency Response | $0 |
| Other Costs | $0 |
Location Map
Incident Narrative
17:55 CONTROLLER ON DUTY RECEIVES SUMP OVERFLOW ALARM AT AVON PUMP STATION WHICH TRIPS AND LOCKED OUT P2. ADJUSTMENTS ARE MADE TO KEEP RICHMOND BOOSTER PUMP ONLINE TO KEEP A MFL INSPECTION TOOL MOVING. 17:57 CONTROLLER CALLS OPERATOR AT BETHANY STATION THAT IS RECEIVING THE MFL INSPECTION TOOL THAT THE AVON PUMP IS DOWN 18:10 OPERATOR CALLS CONTROLLER WHEN ARRIVING AT AVON PUMP STATION. SUMP IS PLACED FROM AUTO INTO LOCAL TO BRING DOWN SUMP LEVELS 18:45 CONTROLLER NOTIFIES OP REP TO INFORM HIM AVON PUMP IS DOWN AND FLOW RATES/PRESSURES ARE BEING MONITORED 19:48 CONTROLLER SPOKE WITH OPERATOR ON SITE AT AVON PUMP STATION WHO STATED THAT THE SUMP LEVEL IS DECREASING AT A SLOWER RATE THAN EXPECTED 20:57 OPERATOR CALLS CONTROLLER NOTIFYING THAT A SECOND EMPLOYEE IS AT AVON PUMP STATION TO ASSIST WITH THE SUMP PUMP 22:44 OPERATOR IDENTIFIES THAT THE SUMP PUMP AT AVON PUMP STATION IS DECREASING AT A SLOWER RATE BECAUSE OF A THERMAL PRESSURE RELIEF VALVE ON THE SUCTION HEADER OF THE PUMP PREMATURELY OPENING, CAUSING THE SUMP TO FILL SUMP TO OVERFLOW. PRV WAS ISOLATED FOR REPAIRS. 00:25 OPERATOR CALLED CONTROL AND SAID HE WAS GOING TO TEST SHUTDOWN SWITCH ON OVERFLOW P2 WENT DOWN IMMEDIATELY.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.