CHEVRON PIPE LINE CO

hazardous_liquid Incident — — April 19, 2019

Incident Information

Incident DateApril 19, 2019
OperatorCHEVRON PIPE LINE CO
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates38.02178, -122.06197

Cause

CauseEQUIPMENT FAILURE
SubcauseMALFUNCTION OF CONTROL/RELIEF EQUIPMENT

Casualties

Fatalities0
Injuries0

Costs

Property Damage$1,500
Emergency Response$0
Other Costs$0

Location Map

Incident Narrative

17:55 CONTROLLER ON DUTY RECEIVES SUMP OVERFLOW ALARM AT AVON PUMP STATION WHICH TRIPS AND LOCKED OUT P2. ADJUSTMENTS ARE MADE TO KEEP RICHMOND BOOSTER PUMP ONLINE TO KEEP A MFL INSPECTION TOOL MOVING. 17:57 CONTROLLER CALLS OPERATOR AT BETHANY STATION THAT IS RECEIVING THE MFL INSPECTION TOOL THAT THE AVON PUMP IS DOWN 18:10 OPERATOR CALLS CONTROLLER WHEN ARRIVING AT AVON PUMP STATION. SUMP IS PLACED FROM AUTO INTO LOCAL TO BRING DOWN SUMP LEVELS 18:45 CONTROLLER NOTIFIES OP REP TO INFORM HIM AVON PUMP IS DOWN AND FLOW RATES/PRESSURES ARE BEING MONITORED 19:48 CONTROLLER SPOKE WITH OPERATOR ON SITE AT AVON PUMP STATION WHO STATED THAT THE SUMP LEVEL IS DECREASING AT A SLOWER RATE THAN EXPECTED 20:57 OPERATOR CALLS CONTROLLER NOTIFYING THAT A SECOND EMPLOYEE IS AT AVON PUMP STATION TO ASSIST WITH THE SUMP PUMP 22:44 OPERATOR IDENTIFIES THAT THE SUMP PUMP AT AVON PUMP STATION IS DECREASING AT A SLOWER RATE BECAUSE OF A THERMAL PRESSURE RELIEF VALVE ON THE SUCTION HEADER OF THE PUMP PREMATURELY OPENING, CAUSING THE SUMP TO FILL SUMP TO OVERFLOW. PRV WAS ISOLATED FOR REPAIRS. 00:25 OPERATOR CALLED CONTROL AND SAID HE WAS GOING TO TEST SHUTDOWN SWITCH ON OVERFLOW P2 WENT DOWN IMMEDIATELY.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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