ENERGY TRANSFER COMPANY
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | ENERGY TRANSFER COMPANY |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 30.68425, -101.27124 |
Cause
| Cause | EQUIPMENT FAILURE |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
AT APPROXIMATELY 2300 HRS. ON MAY 3RD, 2019. ENERGY TRANSFER LIQUIDS CONTROL RECEIVED INDICATIONS OF A LEAK AT PUMP STATION # 3 ON THE S505 WEST TEXAS GATEWAY 16"" NGL PIPELINE. ENERGY TRANSFER LIQUIDS CONTROL CONTACTED ETC OPERATIONS FIELD PERSONNEL TO INVESTIGATE. OPERATIONS TECHNICIANS ARRIVED ON LOCATION AT 12:15 HRS. ON 5/4 AND FOUND A LEAK ON SOME TUBING IN THE STATION. AT 01:25 HRS. THE TECHNICIANS WERE ABLE TO ISOLATE THE LEAK LOCATION BY CLOSING VALVES 7 & 8 ON PUMP # 3 TO ALLOW THE ISOLATED LEAK SECTION TO BLOW DOWN. AN INVESTIGATION FOUND THE 1/2"" TUBING FROM A THERMAL RELIEF ON THE DISCHARGE VALVE ON PUMP # 3 TO BE LOOSE AT THE FITTING. ALL TUBING AND FITTINGS ON THE DISCHARGE VALVE WERE REMOVED AND REPLACED. THE ISOLATION VALVES (7 & 8) WERE OPENED AT 03:41 HRS. AND THE STATION WAS AVAILABLE FOR NORMAL SERVICE AT 04:00 HRS. THE INITIAL REPORT WAS MADE TO THE NRC AT 01:59 HRS. ON MAY 4, 2019, REPORT # 1244598 AND THE NRC 48 HR. UPDATE WAS MADE AT 20:00 HRS. ON MAY 5, 2019, REPORT # 1244739 ETC'S PLAN TO PREVENT REOCCURRENCES OF THIS ISSUE WERE TO REPLACE ALL TUBING AND FITTINGS ON THE DISCHARGE VALVE AND CHECK THE TUBING AND FITTINGS THROUGHOUT THE ENTIRE STATION.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.