ONEOK NGL PIPELINE, LLC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorONEOK NGL PIPELINE, LLC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates41.56536, -93.52586

Cause

CauseINCORRECT OPERATION
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON 8/7/19, THE 101 MAIN FILTER VESSEL BEGAN LEAKING FROM THE SEAL AREA. THE OPERATOR NOTICED A VAPOR CLOUD AROUND THE VESSEL AND PIPELINE CONTROL WAS CALLED TO SHUT DOWN THE PIPELINE. ONCE THE RELEASE STOPPED, THE VESSEL WAS MANUALLY BLOCKED IN AND BLOWN DOWN. A CONTRACTOR WAS CALLED TO THE SITE TO ASSIST MAINTENANCE PERSONNEL WITH INSPECTION OF THE GASKET AND TO RE-TORQUE FLANGE BOLTS. AN ESTIMATED 3.5 BBLS OF PROPANE WERE RELEASED TO ATMOSPHERE. THE VAPOR CLOUD DID NOT LEAVE THE PROPERTY BOUNDARIES. UPDATE: 9/13/19 AFTER COMPLETING THE INVESTIGATION OF THIS INCIDENT, SEVERAL CHANGES HAVE BEEN IMPLEMENTED TO HELP PREVENT THIS INCIDENT FROM OCCURRING AGAIN. THE CURRENT TORQUE PROCEDURES HAVE BEEN UPDATED TO INCLUDE A NEW FLANGE BOLT TIGHTENING SEQUENCE. THIS SEQUENCE HAS ALSO BEEN PLACED ON SIGNS AT EACH INDIVIDUAL FILTER VESSEL. NEW FLANGE BOLTS HAVE BEEN INSTALLED ON THE VESSEL, AND NEW GASKETS HAVE BEEN ORDERED AFTER DETERMINING SHELF LIFE OF THESE GASKETS ARE 2 TO 3 YEARS. ONEOK PERSONNEL AND THE CONTRACTOR USED FOR THIS TASK HAVE BEEN RETRAINED ON THE NEW FLANGE BOLT TIGHTENING PROCEDURE. UPDATED BY: BRENT THEEDE COMPLIANCE SPECIALIST ONEOK, INC.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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