"SFPP, LP"

hazardous_liquid Incident — — March 30, 2021

Incident Information

Incident DateMarch 30, 2021
Operator"SFPP, LP"
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates33.23804, -115.50447

Cause

CauseEQUIPMENT FAILURE
SubcauseDEFECTIVE OR LOOSE TUBING OR FITTING

Casualties

Fatalities0
Injuries0

Costs

Property Damage$300
Emergency Response$45,200
Other Costs$0

Location Map

Incident Narrative

"ON 3/30/21 AT APPROXIMATELY 1424 PST, UNIT #2 ON THE NILAND TO IMPERIAL 6"" (LS58) ACHIEVED A HIGH AMP WARNING AT 70 AMPS BUT DID NOT REACH THE 75 AMP HIGH AMP SHUT-DOWN. OPERATIONS ACKNOWLEDGED THE WARNING AND S/D THE UNIT AT 1431. AT THE SAME TIME THE CONDITION OCCURRED, THE LOCAL LINE RIDER WAS AT THE FACILITY FOR A REGULAR SCHEDULED SITE INSPECTION. THE LINE RIDER RECOGNIZED THE ISSUE AND DETERMINED THERE WAS A RELEASE OF DIESEL AND CALLED THE FIELD CONTROLLER AND AREA MANAGER TO INSURE THE SYSTEM WAS SHUT-DOWN. THE OSRO WAS NOTIFIED IMMEDIATELY AND DISPATCHED TO THE FACILITY. THE RELEASE OCCURRED AS A RESULT OF A FAILED SWAGELOK ""T"" FITTING. UPDATE (7/14/21): THE TUBING DESIGN AND INSTALLATION WAS INADEQUATE FOR THE OPERATING CONDITIONS OF THE UNIT. THE TUBING DESIGN HAD AN UNNECESSARY RECIRCULATING LINE THAT ALLOWED THE ""T"" FITTING UPSTREAM OF THE ISOLATION VALVE TO BE UNDER CONSTANT PRESSURE AND FLOW. IF THE ISOLATION VALVE HAD BEEN INSTALLED UPSTREAM OF THE ""T"" FITTING, THE RELEASE WOULD HAVE BEEN PREVENTED."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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