SUNOCO PIPELINE L.P.

hazardous_liquid Incident — — May 31, 2021

Incident Information

Incident DateMay 31, 2021
OperatorSUNOCO PIPELINE L.P.
CommodityHVL OR OTHER FLAMMABLE OR TOXIC FLUID WHICH IS A GAS AT AMBI
Pipeline Typehazardous_liquid

Location

State
Coordinates40.00690, -75.58410

Cause

CauseEQUIPMENT FAILURE
SubcausePUMP OR PUMP-RELATED EQUIPMENT

Casualties

Fatalities0
Injuries0

Costs

Property Damage$18,000
Emergency Response$4,800
Other Costs$0

Location Map

Incident Narrative

"ON 5/31/21 AT APPROXIMATELY 20:45 CST, HYDROCARBON ALARMS ALERTED PIPELINE CONTROLLER (PC) OF A POTENTIAL HVL LEAK AT THE BOOT PUMP STATION (UNIT BOO3) INSIDE THE PUMP HOUSE. THE PC MADE INTERNAL NOTIFICATIONS, ISOLATED THE PIPELINE FROM THE STATION AND SHUT DOWN THE PUMP. THE PC NOTIFIED THE COUNTY EMS / PSAP TO ADVISE OF AN ALARM INSIDE THE PUMP HOUSE AND THAT COMPANY PERSONNEL WERE RESPONDING. COMPANY PERSONNEL INVESTIGATED THE ALARM. LEAK WAS CONFIRMED AS BOO3 PUMP SEAL LEAK. EQUIPMENT INSIDE THE PUMP HOUSE WAS FURTHER ISOLATED. HVL PRODUCT WAS ROUTED TO THE MAINTENANCE FLARE. NOTE: THE PC NOTIFICATION TO COUNTY EMS / PSAP RESULTED IN EMERGENCY RESPONSE PERSONNEL LOCAL FIRE DEPARTMENT AND COUNTY HAZMAT TEAM RESPONDING TO THE LOCATION TO ASSIST AS NECESSARY. NO OUTSIDE EMERGENCY RESPONSE ASSISTANCE WAS REQUIRED. INVESTIGATION DETERMINED THAT THE SEAL FAILED DUE TO THE INBOARD SEAL SET SCREWS LOOSENING WHICH ALLOWED THE ROTATING SEAL TO AXIALLY SHIFT CAUSING THE SEAL FACES TO CONTACT RESULTING IN DAMAGE TO THE FACES AND O-RING SEAL. THE FAILED SEAL WAS REPLACED AND THE PUMP UNIT WAS INSPECTED FOR ANY OTHER ITEMS THAT COULD LEAD TO SIMILAR REOCCURRENCE. UPON COMPLETION OF INSPECTION THE PUMP UNIT WAS RETURNED TO SERVICE ON 6/3/21."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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