EXPLORER PIPELINE CO

hazardous_liquid Incident —

Incident Information

Report Date
OperatorEXPLORER PIPELINE CO
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates29.71731, -95.18025

Cause

CauseINCORRECT OPERATION
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON DECEMBER 13, 2019, A QUALIFIED EXPLORER PIPELINE EMPLOYEE BECAME DISTRACTED AND LEFT A SMALL BLEEDER VALVE IN THE OPEN POSITION AT THE PASADENA PUMP STATION, AND PRODUCT WAS RELEASED. THE PRODUCT WAS TOTALLY CONTAINED ON THE PROPERTY. ANY IMPACTED SOIL WAS PROPERLY TESTED AND REMOVED. A POST-INCIDENT INTERVIEW WAS IMMEDIATELY CONDUCTED WITH THE OPERATOR BY EXPLORER PIPELINE'S SENIOR AREA MANGER AND MAINTENANCE AND OPERATIONS SUPERVISORS. THE EMPLOYEE ACKNOWLEDGED FAILED TO CLOSE THE BLEEDER VALVE. THE OPERATOR WAS REQUIRED TO COMPLETE A POST-INCIDENT DRUG AND ALCOHOL (D&A) TEST, AND THE MRO CONFIRMED IT WAS NEGATIVE. BEFORE THE EMPLOYEE WAS ALLOWED BACK INTO OPERATIONS, AN EVALUATION WAS COMPLETED BY THE EXPLORER PIPELINE SUPERVISORS. THE EVALUATION CONFIRMED THE EMPLOYEE KNEW THE OPERATIONS IDENTIFIED IN THE PROCEDURE, AND THEY FREQUENTLY CONDUCT OPERATIONS. AN EVALUATION OF THE RECORDS, LOGS, AND QUALIFICATION RECORDS SUPPORTED THAT THE OPERATOR KNEW THE SPECIFICS STEPS. HOWEVER, THE OPERATOR BECAME DISTRACTED WITH THE PHONE CALL FROM THE CONTROL CENTER THAT REQUESTED THE OPERATOR TO CONDUCT A NON-EMERGENCY SHUTDOWN. AFTER CONSULTATION, THE SENIOR MANAGEMENT ELECTED TO CONDUCT COUNSELING WITH THE OPERATOR BEFORE THEY RETURNED TO OPERATIONS VERSUS UNDERGOING A FULL OQ REQUALIFICATION.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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