COLONIAL PIPELINE CO
hazardous_liquid Incident — — August 11, 2021
Incident Information
| Incident Date | August 11, 2021 |
| Operator | COLONIAL PIPELINE CO |
| Commodity | REFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 29.71860, -95.17955 |
Cause
| Cause | EQUIPMENT FAILURE |
| Subcause | "FAILURE OF EQUIPMENT BODY (EXCEPT PUMP), TANK PLATE, OR OTHER MATERIAL" |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | $0 |
| Emergency Response | $204,228 |
| Other Costs | $0 |
Location Map
Incident Narrative
"ON 8/11/21, AT APPROXIMATELY 00:36, A HOUSTON (HTN) COLONIAL OPERATOR SMELLED PRODUCT CONDUCTING A YARD CHECK AND BEGAN INVESTIGATING THE SOURCE. THE OPERATOR NOTICED STAINED ROCKS SURROUNDING THE LINE 2 (L2) EVA SHIPPER VALVE. THIS LED THE OPERATOR TO OBSERVE ULTRA LOW SULFUR DIESEL (ULSD) IN 3 ACCESS WELLS NEXT TO THE VALVE. THE OPERATOR INFORMED THE ON-SHIFT A & B OPERATORS. HTN L2 WAS SHUTDOWN PENDING INVESTIGATION OF THE LEAK SOURCE AND NOTIFICATIONS WERE MADE TO APPROPRIATE PERSONNEL. OPERATIONS AT THIS VALVE REQUIRED FURTHER INVESTIGATION TO DETERMINE THE RESPONSIBLE PARTY. A POTENTIAL RESPONSIBLE PARTY SUBMITTED A NRC CALL (NRC INCIDENT REPORT # 1313343). THE SUMMARY OF THIS CALL INCLUDED JOINT INVESTIGATION ACTIONS UNDERWAY TO DETERMINE THE LEAK SOURCE AND RESPONSIBLE PARTY. 8/12/21, COLONIAL CONFIRMED OWNERSHIP OF THE LEAK SOURCE (RESPONSIBLE PARTY). COLONIAL FOUND THE LEAK TO BE A RESULT OF A VALVE BODY GUIDE PLUG MALFUNCTION. AT APPROXIMATELY 11:00 CST, COLONIAL DISCOVERED THE SPILL RESPONSE COSTS MAY EXCEED $50,000 AND MADE A NOTIFICATION TO THE NRC (NRC INCIDENT REPORT #1313487). ADDITIONALLY, PHMSA AID WAS CONTACTED TO CLARIFY INCIDENT REPORT # 1313343 DISCUSSED ABOVE WAS THE SAME LEAK. OTHER NOTIFICATIONS WERE MADE AS REQUIRED. APPROXIMATELY 100 GALLONS OF ULSD WAS RELEASED AND CONTAINED ONSITE. ON 8/14/2021, COLONIAL CONDUCTED A 48 HOUR UPDATED NOTIFICATION TO NRC INCIDENT # 1313487. THIS NOTIFICATION REPORTED NO SIGNIFICANT CHANGES OTHER THAN THE VALVE REPAIR WAS COMPLETED ON 8/13/21. AN IA WILL BE CONDUCTED FOR THIS INCIDENT."
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.