"BUCKEYE PARTNERS, LP"

hazardous_liquid Incident — — February 11, 2022

Incident Information

Incident DateFebruary 11, 2022
Operator"BUCKEYE PARTNERS, LP"
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates40.55685, -74.41329

Cause

CauseNATURAL FORCE DAMAGE
SubcauseTEMPERATURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$0
Emergency Response$36,800
Other Costs$2,800

Location Map

Incident Narrative

"ON FEBRUARY 11, 2022 AT APPROXIMATELY 13:44 EST LOCAL OPERATIONS WAS CONDUCTING ROUTINE MAINTENANCE AT SOUTH PLAINFIELD VALVE SITE AND NOTICED A STRONG SMELL OF GASOLINE. UPON FURTHER INVESTIGATION, SHEEN ON WATER WAS NOTICED IN THE CONCRETE CONTAINMENT VAULT. ALL INSIDE AND OUTSIDE NOTIFICATIONS WERE MADE. THE CONTROL CENTER WAS NOTIFIED TO SHUT DOWN IN A CONTROLLED MANOR AND ISOLATE THE LINE SECTION. A BOOM WAS PLACED INSIDE THE VAULT AROUND THE VALVE BODY AS AN EXTRA PRECAUTION. LOCAL OSRO ARRIVED ON SITE. APPROXIMATELY 3100 GALLONS OF WATER/GASOLINE MIX WAS RECOVERED AND SEPARATED. ESTIMATED AMOUNT OF GASOLINE RELEASED AFTER SEPARATION WAS APPROXIMATELY 11 GALLONS. THE DRAIN PLUG LOCATED ON THE VALVE BODY WAS DETERMINED TO BE LOOSE AND SEEPING PRODUCT. THE DRAIN PLUG WAS TIGHTENED. THERE WAS NO VISIBLE DAMAGE OR CORROSION TO THE DRAIN PLUG. THE FREEZE/THAW CYCLE AND EXTREME TEMPERATURE CHANGES CAUSED THE DRAIN PLUG TO LOOSEN AND SLIGHTLY BACKOUT. PIPELINE RETURNED TO NORMAL OPERATIONS."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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