MPLX LP
hazardous_liquid Incident — — October 14, 2022
Incident Information
| Incident Date | October 14, 2022 |
| Operator | MPLX LP |
| Commodity | HVL OR OTHER FLAMMABLE OR TOXIC FLUID WHICH IS A GAS AT AMBI |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 39.95621, -80.52594 |
Cause
| Cause | EQUIPMENT FAILURE |
| Subcause | OTHER EQUIPMENT FAILURE |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | $0 |
| Emergency Response | $0 |
| Other Costs | $34,000 |
Location Map
Incident Narrative
"10/14/2022 13:40 STOPPLE COMPLETION PLUG WAS SET, AND TDW WAS REMOVING THE COMPLETION PLUG INSTALLATION CONE 13:45 BALL CHECK INTERNAL TO THE COMPLETION PLUG STARTED TO LEAK 13:58 UPSTREAM VALVE WAS SHUT TO ISOLATE INCOMING FLOW, LINE PACK WAS PULLED DOWN TO THE LOWEST PRESSURE POSSIBLE 14:15 DOWNSTREAM ISOLATION VALVE SHUT 21:00 NITROGEN WAS USED TO PURGE THE PIPELINE OF PRODUCT 10/15/2022 10:00 REPAIRS WERE COMPLETED 12:00 PIPELINE WAS PURGED BACK INTO SERVICE"
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.