SCM PR, LLC

hazardous_liquid Incident — — March 2, 2021

Incident Information

Incident DateMarch 2, 2021
OperatorSCM PR, LLC
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates43.64802, -105.64191

Cause

CauseEQUIPMENT FAILURE
SubcauseNON-THREADED CONNECTION FAILURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$10,000
Emergency Response$80,000
Other Costs$0

Location Map

Incident Narrative

SATELLITE COMMUNICATIONS HAD BEEN LOST SUCH THAT PRESSURE READINGS WERE NOT BEING REPORTED TO THE OPERATIONS CENTER FROM THE TWO PIPELINES THAT FLOW TO THE LACT UNIT AT THE STATION. ONE LINE IS THE 12"" OUTRIGGER (REGULATED) AND THE OTHER IS THE 8"" FOXTAIL (UNREGULATED). THE CONTROLLER DID NOT ALERT FIELD PERSONNEL OF THE SITUATION IN A TIMELY MANNER AND DID NOT SHUT DOWN THE PUMP STATION CONTROLLING FLOW ON THE 8"" FOXTAIL LINE. A TRUCK DRIVER UNLOADING CRUDE AT ANOTHER RECEIVING POINT AT THE STATION REPORTED THE RELEASE TO OUR OPERATIONS CENTER AND PRODUCERS WERE NOTIFIED TO STOP DELIVERIES. THE GASKET TO THE STRAINER BASKET IN THE LACT UNIT HAD FAILED AND WAS THE SOURCE OF THE RELEASE. THIS LACT WAS INSTALLED IN 2016; AND, GASKET IS REMOVED AND EXAMINED EVERY TWO WEEK. A WRENCH WITH GREATER TORQUE IS BEING ORDER FOR MANAGING THE MAINTENANCE OF THIS CLOSURE SERVED BY THE GASKET. EXACT PRESSURE AT THE LACT UNIT IS NOT KNOWN DUE TO THE LOSS OF SATELLITE COMMUNICATIONS - NO PRESSURES WERE CAPTURED.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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