ENTERPRISE CRUDE PIPELINE LLC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorENTERPRISE CRUDE PIPELINE LLC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates31.87875, -102.12596

Cause

CauseINCORRECT OPERATION
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON 4/12/2021, AFTER PRODUCT MOVEMENT WAS SHUT DOWN, THE PIPELINE CONTROLLER NOTICED THE SUMP TANK CONTINUED TO BE FILLED AND CONTACTED LOCAL OPERATIONS TO INVESTIGATE. AT 6:45 AM, A TECHNICIAN ARRIVED AND DISCOVERED OIL OVERFLOWING FROM THE PROVER BOX AT BRYANT G SOUTH STATION. THE TECHNICIAN ISOLATED THE METER SKID AND THE LEAK WAS STOPPED. AT 8:00 AM, IT WAS DETERMINED THE RELEASE MET ACCIDENT REPORTING CRITERIA BASED ON THE ESTIMATED VOLUME OF CRUDE RELEASED. THE TRRC WAS NOTIFIED AT 8:48 AM, INCIDENT #2410. INVESTIGATION IDENTIFIED THAT A VALVE WAS UNINTENTIONALLY LEFT PARTIALLY OPEN, ALLOWING CRUDE OIL TO DRAIN FROM THE MAINLINE INTO THE PROVER LOOP AND THEN OVERFLOWED THE SUMP. THE INVESTIGATION COULD NOT CLEARLY IDENTIFY WHEN THE VALVE WAS LAST OPERATED OR BY WHOM. TO PREVENT RECURRENCE A LARGER DIAMETER DRAIN LINE SYSTEM HAS BEEN INSTALLED TO CAPTURE OVERFILL FROM THE PROVER BOX AND DIRECT IT TO THE SUMP. SOIL REMEDIATION HAS BEEN COMPLETED.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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