ENTERPRISE CRUDE PIPELINE LLC
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | ENTERPRISE CRUDE PIPELINE LLC |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 31.87875, -102.12596 |
Cause
| Cause | INCORRECT OPERATION |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
ON 4/12/2021, AFTER PRODUCT MOVEMENT WAS SHUT DOWN, THE PIPELINE CONTROLLER NOTICED THE SUMP TANK CONTINUED TO BE FILLED AND CONTACTED LOCAL OPERATIONS TO INVESTIGATE. AT 6:45 AM, A TECHNICIAN ARRIVED AND DISCOVERED OIL OVERFLOWING FROM THE PROVER BOX AT BRYANT G SOUTH STATION. THE TECHNICIAN ISOLATED THE METER SKID AND THE LEAK WAS STOPPED. AT 8:00 AM, IT WAS DETERMINED THE RELEASE MET ACCIDENT REPORTING CRITERIA BASED ON THE ESTIMATED VOLUME OF CRUDE RELEASED. THE TRRC WAS NOTIFIED AT 8:48 AM, INCIDENT #2410. INVESTIGATION IDENTIFIED THAT A VALVE WAS UNINTENTIONALLY LEFT PARTIALLY OPEN, ALLOWING CRUDE OIL TO DRAIN FROM THE MAINLINE INTO THE PROVER LOOP AND THEN OVERFLOWED THE SUMP. THE INVESTIGATION COULD NOT CLEARLY IDENTIFY WHEN THE VALVE WAS LAST OPERATED OR BY WHOM. TO PREVENT RECURRENCE A LARGER DIAMETER DRAIN LINE SYSTEM HAS BEEN INSTALLED TO CAPTURE OVERFILL FROM THE PROVER BOX AND DIRECT IT TO THE SUMP. SOIL REMEDIATION HAS BEEN COMPLETED.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.