"ONEOK NGL PIPELINE, LLC"

hazardous_liquid Incident — — May 12, 2023

Incident Information

Incident DateMay 12, 2023
Operator"ONEOK NGL PIPELINE, LLC"
CommodityHVL OR OTHER FLAMMABLE OR TOXIC FLUID WHICH IS A GAS AT AMBI
Pipeline Typehazardous_liquid

Location

State
Coordinates32.69511, -103.28143

Cause

CauseEQUIPMENT FAILURE
SubcauseNON-THREADED CONNECTION FAILURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$100
Emergency Response$500
Other Costs$0

Location Map

Incident Narrative

"ON MAY 13, 2023 AT 10:50AM (MDT) ONEOK PIPELINE CONTROL RECEIVED A CALL FROM A 3RD PARTY OPERATOR WHO REPORTED A POTENTIAL ICE BALL AT ONEOK LINAM RANCH METER SKID. A ONEOK OPERATOR WAS DISPATCHED AND ARRIVED ON SITE TO DISCOVER A RELEASE ON THE ONEOK LAUNCHER DOOR. THE LAUNCHER WAS ISOLATED AND EVACUATED OF PRODUCT. UPON INVESTIGATION, THE OPERATOR FOUND THE LAUNCHER DOOR O-RING HAD FAILED. THE O-RING WAS REPLACED, PRODUCT REINTRODUCED TO THE LAUNCHER WITH THE OPERATOR REMAINING ON SITE TO ENSURE NORMAL OPERATIONS. ONEOK REVIEWED PRESSURE TRANSMITTER DATA AND DETERMINED THE O-RING FAILURE LIKELY STARTED AT APPROXIMATELY 5:50 PM ON MAY 12TH. UPDATE: ONEOK SUBMITTED THE FAILED O-RING TO A THIRD PARTY FOR ANALYSIS. THE THIRD PARTY ANALYSIS DETERMINED THE O-RING FAILED DUE TO A DECOMPRESSION EVENT AND DID NOT FIND ANY INDICATION OF O-RING MATERIAL DEGRADATION. THE O-RING MATERIAL ITSELF, AS COMPARED TO AN EXEMPLAR, APPEARED TO HAVE MAINTAINED ELASTICITY, HAD APPROPRIATE HARDNESS, APPROPRIATE CHEMICAL ANALYSIS, AND A 1.1 PERCENT DEVIATION IN THE O-RING CIRCUMFERENCE MEASUREMENT. THE LAB WAS NOT ABLE TO DETERMINE THE CAUSE OF THE DECOMPRESSION EVENT. ONEOK VERIFIED THE O-RING WAS INSTALLED PER ONEOK'S PROCEDURE."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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