"PALO DURO TEG, LLC"

hazardous_liquid Incident — — August 14, 2023

Incident Information

Incident DateAugust 14, 2023
Operator"PALO DURO TEG, LLC"
CommodityHVL OR OTHER FLAMMABLE OR TOXIC FLUID WHICH IS A GAS AT AMBI
Pipeline Typehazardous_liquid

Location

State
Coordinates32.72728, -97.94838

Cause

CauseMATERIAL FAILURE OF PIPE OR WELD
SubcauseORIGINAL MANUFACTURING-RELATED (NOT GIRTH WELD OR OTHER WELDS FORMED IN THE FIELD)

Casualties

Fatalities0
Injuries0

Costs

Property Damage$175,000
Emergency Response$0
Other Costs$0

Location Map

Incident Narrative

"OPERATIONS WAS NOTIFIED OF A POTENTIAL LEAK BY A THIRD-PARTY OPERATOR THAT SHARES A COMMON PIPELINE CORRIDOR. OPERATIONS WAS NOTIFIED AND INITIATED A FIELD INVESTIGATION. THE POTENTIAL LEAK WAS VERIFIED IN THE FIELD. OPERATIONS MADE INTERNAL NOTIFICATIONS. A DIG WAS INITIATED, THE PIPE WAS EXPOSED, AND THE LEAK WAS CONFIRMED. PRODUCERS MIDSTREAM UTILIZED STOPPLES TO ISOLATE AND MANAGE THE AMOUNT OF PRODUCT LOST. UPSTREAM AND DOWNSTREAM MAIN LINE VALVES WERE ALSO ISOLATED DURING THE REPAIR TO IMPLEMENT DOUBLE BLOCK AND BLEED. IT IS OUR BELIEF THAT THE 295 BARRELS LOST IS A WORST-CASE SCENARIO. THIS VALUE WAS GENERATED USING LEAK CALCULATIONS FROM PROMAX. THE ACTUAL LEAK AMOUNT IS BELIEVED TO BE SOMEWHERE BETWEEN 16 AND 295 BARRELS. WE DEDUCED BECAUSE OF THE MINIMAL CONTAMINATION OF THE SOIL THAT WAS CONFIRMED BY A THIRD-PARTY LAB ANALYSIS. THE FAILED PIPE WAS EXCAVATED, AND THE ENTIRE JOINT WAS REMOVED. PRODUCERS MIDSTREAM SENT THE FAILED PIPE TO AN INDEPENDENT LAB FOR FURTHER ANALYSIS ON AN EXPEDITE SCHEDULE. THE NEW PIPE WAS TESTED, INSTALLED, AND THE LINE WAS PURGED BACK INTO SERVICE UPON REMOVAL OF THE STOPPLES."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

Back to All Incidents More Incidents in