IRONWOOD MIDSTREAM ENERGY PARTNERS, LLC

hazardous_liquid Incident — — January 25, 2022

Incident Information

Incident DateJanuary 25, 2022
OperatorIRONWOOD MIDSTREAM ENERGY PARTNERS, LLC
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates29.01429, -97.84505

Cause

CauseEQUIPMENT FAILURE
SubcauseMALFUNCTION OF CONTROL/RELIEF EQUIPMENT

Casualties

Fatalities0
Injuries0

Costs

Property Damage$2,000
Emergency Response$500
Other Costs$0

Location Map

Incident Narrative

KINDER MORGAN HELENA TERMINAL INLET CONTROL VALVE STOPPED RESPONDING AND GOT STUCK AT 18% OPEN. THIS CAUSED THE PIPELINE TO PRESSURE UP. THE BALON 4"" - 600# CHECK VALVE DID NOT HOLD CAUSING PRESSURE TO COME BACK THROUGH THE PUMP AND BLOW OUT THE O-RING ON THE SUCTION STRAINER BASKET. THE LACT UNIT SKID PIPING NEVER EXCEEDED 69 PSIG. ALL OTHER PIPING AND EQUIPMENT WAS THOROUGHLY INSPECTED AND NO OTHER DAMAGE WAS DISCOVERED. OPERATOR WILL BE REPLACING FAILED CHECK VALVE WITH A DIFFERENT MAKE AND MODEL WHICH FACILITATES FOR EASIER ROUTINE MAINTIENCE, TO PREVENT A REOCCURRENCE.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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