ROSE ROCK MIDSTREAM OPERATING, LLC

hazardous_liquid Incident — — February 10, 2022

Incident Information

Incident DateFebruary 10, 2022
OperatorROSE ROCK MIDSTREAM OPERATING, LLC
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates38.33295, -98.18400

Cause

CauseEQUIPMENT FAILURE
SubcauseNON-THREADED CONNECTION FAILURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$1,000
Emergency Response$1,024
Other Costs$0

Location Map

Incident Narrative

AT 8AM ON THURSDAY, FEBRUARY 10TH, THE STATION OPERATOR ARRIVED AT THE LYONS STATION AND AS HE ENTERED THE FACILITY, HE NOTICED CRUDE OIL ON THE GROUND BY THE METER SAMPLER. THE STATION OPERATOR CALLED THE CONTROL CENTER TO SHUT DOWN THE STATION PUMPS. UPON INVESTIGATING THE SCENE, THE STATION OPERATOR WAS ABLE TO CLOSE A 1/2-INCH BALL VALVE GOING TO THE SAMPLE SOLENOID, WHICH STOPPED THE LEAK. AFTER THE LEAK WAS ISOLATED AND CONTAINED, REMEDIATION EFFORTS SOON COMMENCED WITH ALL CRUDE OIL CONTAMINATED SOIL COLLECTED IN 55GAL DRUMS AND SENT FOR DISPOSAL. DURING THE INVESTIGATION OF THE SAMPLER UNIT, IT WAS DETERMINED THAT AN O-RING HAD FAILED CAUSING CRUDE OIL TO ESCAPE FROM THE UNIT. THE O-RING WAS REPLACED, AND THE FAILURE WAS MITIGATED.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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