ENABLE GAS GATHERING, LLC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorENABLE GAS GATHERING, LLC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates35.22688, -97.83172

Cause

CauseCORROSION FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON FEBRUARY 20TH, 2022 AT 15:45 ENABLE GAS GATHERING LINE V-6 EXPERIENCED A LEAK IN GRADY COUNTY OKLAHOMA. THE LEAKING CRUDE OIL MIGRATED TO A NEARBY POND WHERE IT WAS DISCOVERED BY THE LANDOWNER. THE LANDOWNER NOTIFIED EGG SYSTEM CONTROL AND OPERATIONS PERSONNEL WERE DISPATCHED. OPS PERSONNEL WERE ABLE TO CONFIRM THE LEAK WAS ON LINE V-6. THE UPSTREAM AND DOWNSTREAM VALVES WERE CLOSED AND THE SECTION OF LINE WAS ISOLATED. ALL OIL WAS CONTAINED AND SPILL CONTRACTORS WERE CONTACTED AND ASSEMBLED ONSITE TO BEGIN REMEDIATION. THE PIPELINE WAS REPAIRED WITH A PLIDCO CLAMP ON 2/21/22 AND PLACED BACK INTO SERVICE ON 2/22/22. THE NRC WAS NOTIFIED ON 2/20/2022 (NRC # 1329326). A 48-HR FOLLOW UP CALL WAS PROVIDED TO THE NRC ON 2/22/2022 (NRC # 1329476). THE PIPE WAS CUT OUT AND REPLACED. EXAMINATION CONFIRMED THE FAILURE WAS DUE TO INTERNAL CORROSION. THE COMPANY HAS IMPLEMENTED ADDITIONAL CLEANING PIG TOOL RUNS AND WILL BEGIN TREATING THE LINE WITH A CORROSION INHIBITOR AND BIOCIDE.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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