DELEK CRUDE LOGISTICS, LLC.
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | DELEK CRUDE LOGISTICS, LLC. |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 33.04505, -96.12157 |
Cause
| Cause | CORROSION FAILURE |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
A CALL WAS RECEIVED IN THE CONTROL CENTER FROM A LANDOWNER WHO INDICATED THERE WAS A SMELL OF DIESEL. THE LINE WAS SHUTDOWN AT 12:15 ON 3/28/22 AND FIELD PERSONNEL DISPATCHED. UPON ARRIVAL AT THE SITE AT 13:15 ON 3/28/22, FIELD PERSONNEL CONFIRMED A RELEASE, WITH DEAD VEGETATION AND MINOR SURFACE PRODUCT. RESPONSE PERSONNEL WERE DISPATCHED TO THE SITE. THE RELEASE SOURCE WAS EXPOSED AND IDENTIFIED AS A PINHOLE LEAK UNDER DIS-BONDED COATING. THE LEAK WAS REPAIRED WITH A TEMPORARY CLAMP FOR CLEANUP, AND CUT OUT AT A LATER DATE. UT ILI TOOLS WERE RUN THROUGH THE AFFECTED SECTION OF PIPE IN OCTOBER OF 2021 AND AGAIN IN DECEMBER OF 2021. NEITHER TOOL RUN IDENTIFIED EXTERNAL METAL LOSS AT THE LEAK SITE. THE PIPELINE HAS BEEN PURGED WITH NITROGEN AND WILL REMAIN HYDROCARBON FREE UNTIL ADDITIONAL TESTS ARE PERFORMED TO ENSURE THE INTEGRITY OF THE LINE.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.