ENABLE GAS GATHERING, LLC
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | ENABLE GAS GATHERING, LLC |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 35.26026, -97.83576 |
Cause
| Cause | CORROSION FAILURE |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
ON APRIL 8TH, 2022 AT 18:35 ENABLE GAS GATHERING LINE V-6 EXPERIENCED A LEAK IN GRADY COUNTY OKLAHOMA. THE LEAKING CRUDE OIL MIGRATED TO A NEARBY DRAINAGE DITCH WHICH LEADS TO A POND WHERE IT WAS DISCOVERED BY THIRD PARTY FLAGGING CREW. OPS PERSONNEL WERE ABLE TO CONFIRM THE LEAK WAS ON LINE V-6. THE UPSTREAM AND DOWNSTREAM VALVES WERE CLOSED AND THE SECTION OF LINE WAS ISOLATED. ALL OIL WAS CONTAINED AND SPILL CONTRACTORS WERE CONTACTED AND ASSEMBLED ONSITE TO BEGIN REMEDIATION. THE NRC WAS NOTIFIED ON 4/8/2022 (NRC # 1333087). A 48-HR FOLLOW UP CALL WAS PROVIDED TO THE NRC ON 4/10/2022 (NRC # 1333199). THE PIPELINE WAS RESTARTED ON 05/11/2022 08:10 WITH A 20% PRESSURE REDUCTION. THE PIPE WAS CUT OUT AND REPLACED. EXAMINATION CONFIRMED THE FAILURE WAS CONFIRMED TO BE DUE TO INTERNAL CORROSION. THE COMPANY HAS IMPLEMENTED ADDITIONAL CLEANING PIG TOOL RUNS AND TREATMENT OF THE LINE WITH A CORROSION INHIBITOR AND BIOCIDE.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.