ENTERPRISE PRODUCTS OPERATING LLC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorENTERPRISE PRODUCTS OPERATING LLC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates30.48158, -97.39943

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

AT 18:27 ON 5/26/2022 ENTERPRISE HOUSTON CONTROL CENTER (HCC) RECEIVED A HAZARDOUS GAS DETECTION ALARM AT COUPLAND PUMP STATION ON THE SEMINOLE BLUE MAINLINE. AN ENTERPRISE TECHNICIAN ARRIVED ON SITE AT 19:25 AND CONFIRMED A RELEASE FROM THE SEMINOLE BLUE PUMP HEADER. AT THAT TIME HCC SHUT DOWN THE PUMP STATION AND THE UPSTREAM ISOLATION VALVE. THE SOURCE OF THE LEAK APPEARED TO BE THE #2 PUMP SUCTION VALVE, AND AT 20:20 THE DETERMINATION WAS MADE THAT THE LEAK WAS REPORTABLE TO THE NRC ON THE BASIS OF ANTICIPATED VALVE REPAIR/REPLACEMENT COSTS EXCEEDING $50,000. THE MANUAL ISOLATION VALVE DOWNSTREAM OF COUPLAND STATION COULD NOT BE CLOSED UNTIL THE PRESSURE WAS SUFFICIENTLY PULLED DOWN BY DOWNSTREAM PUMPS, WHICH RESULTED IN THE VALVE BEING CLOSED AT APPROXIMATELY 21:00. AT 22:10 ENTERPRISE PERSONNEL DETERMINED THAT THE SOURCE OF THE LEAK WAS A FAILED 1/2 INCH PRESSURE SAFETY VALVE (PSV) ON THE SUCTION VALVE BODY, INSTEAD OF THE SUCTION VALVE ITSELF. THE PSV WAS REPLACED AT A COST SIGNIFICANTLY LOWER THAN $50,000. THE LINE WAS RESTORED TO SERVICE ON 5/27/2022 AT 01:11. ORIGINAL NRC REPORT #1337120, 48-HOUR UPDATE #1337217. THE LOWER REPAIR COST WAS REPORTED TO NRC DURING THE 48-HOUR UPDATE. IN ADDITION, PHMSA AID WAS NOTIFIED OF THE LOWER REPAIR COST.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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