ENBRIDGE ENERGY, LIMITED PARTNERSHIP
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | ENBRIDGE ENERGY, LIMITED PARTNERSHIP |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 40.94296, -88.64723 |
Cause
| Cause | INCORRECT OPERATION |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
ON JUNE 23, 2022 AT APPROXIMATELY 2:20 PM CDT, WHILE PERFORMING OPEN SYSTEM MAINTENANCE WORK, CREWS EXPERIENCED A RELEASE OF 7 BARRELS OF CRUDE OIL WITHIN MANIFOLD 201 AT FLANAGAN TERMINAL DUE TO A PASSING ISOLATION VALVE. INCOMING AND OUTGOING LINES AT FLANAGAN TERMINAL WERE ALREADY SHUT DOWN FOR SCHEDULED MAINTENANCE ACTIVITIES. PLM CREWS WERE ON-SITE WITH VAC TRUCKS TO RECOVER IMPACTED SOIL. A CONTRACTOR WAS ALSO MOBILIZED WITH ADDITIONAL CLEAN UP AND RECOVERY EQUIPMENT. THE NRC WAS NOTIFIED ON JUNE 23, 2022 AT 3:05 PM CDT (REPORT #1339619). A 48-HOUR NRC NOTIFICATION WAS MADE ON JUNE 25, 2022 AT 12:11 PM CDT (REPORT #1339763). THE CAUSE OF THE RELEASE WAS DUE TO INCORRECTLY DISASSEMBLING A FLANGE CONNECTION ON VALVE 201-V-2023. THE VALVE WAS REPAIRED, AND ALL LINES WERE RETURNED TO SERVICE. APPROXIMATELY 12 YARDS OF CONTAMINATED SOIL WAS REMOVED FROM THE RELEASE SITE.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.