ENTERPRISE PRODUCTS OPERATING LLC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorENTERPRISE PRODUCTS OPERATING LLC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates29.68956, -95.05709

Cause

CauseINCORRECT OPERATION
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON 8/17/22, AT 7:05 AM, CONTRACTORS NOTIFIED ENTERPRISE OF A LEAK INSIDE THE CHANNEL METER STATION. AT 07:15 AM, ENTERPRISE PERSONNEL ARRIVED ON SITE AND CONFIRMED THE LEAK WAS ON THE CHANNEL 8"" LINE. AT 08:05 AM, THE EMERGENCY RESPONSE TEAM ARRIVED WITH THE REQUIRED PERSONAL PROTECTIVE EQUIPMENT NEEDED TO ENTER THE SITE. AT 08:15 AM, THE LEAK SOURCE WAS IDENTIFIED TO BE A PRESSURE GAUGE ON PIPING INSTALLED FOR THE ILI ASSESSMENT. A VALVE UPSTREAM WAS CLOSED, ENDING THE RELEASE. THE PRESSURE GAUGE WAS REMOVED AND REPLACED WITH A PLUG. AT 07:50 AM, ENTERPRISE DETERMINED THE LEAK VOLUME EXCEEDED 5 GALLONS AND NOTIFIED THE TRRC AT 08:29 AM, INCIDENT REPORT NUMBER 2685. NRC REPORTING CRITERIA WAS NOT MET. INVESTIGATION OF THE FAILURE CONCLUDED THAT THE PRESSURE GAUGE HAD A LOWER PRESSURE SCALE RANGE THAN THE PIPELINE'S OPERATING PRESSURE. THE PRESSURE GAUGE FAILED UPON EXCEEDANCE OF ITS TOP RANGE OF 600 PSIG. THE CONTRACTOR DID NOT CONDUCT A DRUG OR ALCOHOL TEST AS THE PRESSURE GAUGE WAS INSTALLED 38 HOURS PRIOR TO THE ACCIDENT.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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