COLONIAL PIPELINE CO

hazardous_liquid Incident — — December 9, 2024

Incident Information

Incident DateDecember 9, 2024
OperatorCOLONIAL PIPELINE CO
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates33.73922, -85.17150

Cause

CauseEQUIPMENT FAILURE
SubcauseNON-THREADED CONNECTION FAILURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$200,000
Emergency Response$869,103
Other Costs$0

Location Map

Incident Narrative

"ON DECEMBER 9, 2024 AN INCREASE IN PRODUCT LEVELS WAS OBSERVED IN A MONITOR WELL IN THE BREMEN BOOSTER STATION. INVESTIGATIVE POTHOLING LED TO THE DISCOVERY OF AN ACTIVE LEAK SOURCE. THE PRIMARY FAILURE IS BELIEVED TO BE A SOFT GOODS ISSUE WITH FAILED O-RING(S) ON THE BOTTOM END OF THE CLAPPER SHAFT ASSEMBLY OF A STATION CHECK VALVE. THE VALVE WAS REMOVED FROM THE SYSTEM."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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