ENABLE GAS GATHERING, LLC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorENABLE GAS GATHERING, LLC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates34.98613, -97.77491

Cause

CauseCORROSION FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON 5/3/2023 AT 09:40, THE CONTROL CENTER RECEIVED A CALL FROM A LANDOWNER STATING OIL WAS OBSERVED ON THE SURFACE NEAR THE VLC-3 PIPELINE. THE PIPELINE WAS IMMEDIATELY SHUT DOWN AND LOCAL PIPELINE OPERATIONS PERSONNEL WERE DISPATCHED TO THE AREA. AT APPROXIMATELY 10:30, THE LEAK WAS LOCATED AND APPROXIMATELY 14:00, THE LEAK WAS CONFIRMED TO BE COMING FROM THE VLC-3 CRUDE PIPELINE. APPROXIMATELY 205 BARRELS OF CRUDE OIL WAS RELEASED. THE PRODUCT TRAVELLED TO AN UNKNOWN TRIBUTARY AND CONTINUED INTO A SMALL POND. ADDITIONAL PERSONNEL WERE SENT TO THE SITE TO BEGIN OIL RESPONSE RECOVERY EFFORTS, ALONG WITH VACUUM TRUCKS AND OSROS. AT 15:15, A PLIDCO MECHANICAL CLAMP WAS INSTALLED TO PREVENT ANY FURTHER RELEASE. THE PIPELINE WAS MONITORED OVERNIGHT FOR ANY ADDITIONAL RELEASE. ON 5/10/23, AN ILI TOOL RUN WAS PERFORMED. PERMANENT REPAIRS WILL BE DETERMINED PENDING TOOL RUN RESULTS. A SUPPLEMENTAL REPORT WILL BE SUBMITTED ONCE THE INVESTIGATION AND CAUSAL DETERMINATION IS COMPLETE. SUPPLEMENTAL/FINAL: THE PERMANENT REPAIR OF THE PIPELINE WAS COMPLETED ON 8/29/23; REPLACED APPROXIMATELY 20 FEET OF PIPE INCLUDING THE FAILED SECTION AND PLIDCO MECHANICAL CLAMP. THE INVESTIGATION DETERMINED THE CAUSE OF THE ACCIDENT WAS DUE TO INTERNAL CORROSION. CLEANING PIGS ARE NOW BEING USED TO PREVENT REOCCURRENCE.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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