TARGA DOWNSTREAM LLC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorTARGA DOWNSTREAM LLC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates32.01932, -96.78338

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON 5/14/2023, AT APPROXIMATELY 17:10, TARGA NGL CONTROL ROOM RECEIVED 3 GAS DETECTOR ALARMS AT THE NAVARRO PUMP STATION (PS9). CONTROLLER IMMEDIATELY DISPATCHED I&E TECHNICIAN TO LOCATION TO INVESTIGATE. I&E TECHNICIAN ARRIVED AT APPROXIMATELY 18:45 AND IDENTIFIED A RELEASE FROM THE RECEIVER PIG TRAP CLOSURE. UPON ARRIVAL, AND QUICK INVESTIGATION OF THE SITUATION, I&E TECHNICIAN DETERMINED THE ACTUATOR STOPS WERE OUT OF ADJUSTMENT WHICH CAUSED THE VALVE NOT TO BE FULLY SEATED IN THE CLOSED POSITION. AS A RESULT, WHEN THE O-RING FAILED, A SMALL AMOUNT OF PRODUCT LEAKED PAST THE FAILED O-RING. ACTUATOR STOPS WERE ADJUSTED AND PRODUCT FLOW STOPPED. TRAP CLOSURE O-RING WAS REPLACED AND TRAP RETURNED TO NORMAL OPERATING CONDITION. TARGA OPERATIONS HAS IDENTIFIED ISSUES WITH THIS ACTUATOR AND HAS ALREADY BEGUN INSTALLING ANCILLARY EQUIPMENT IN PREPARATION FOR NEW ACTUATOR FROM A NEW MANUFACTURE. DUE TO LEAD TIME, NEW ACTUATOR IS ESTIMATED TO BE INSTALLED BEFORE THE END OF THE YEAR.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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