NUSTAR PIPELINE OPERATING PARTNERSHIP L.P.
hazardous_liquid Incident — — May 8, 2025
Incident Information
| Incident Date | May 8, 2025 |
| Operator | NUSTAR PIPELINE OPERATING PARTNERSHIP L.P. |
| Commodity | HVL OR OTHER FLAMMABLE OR TOXIC FLUID WHICH IS A GAS AT AMBI |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 35.02480, -91.93210 |
Cause
| Cause | EQUIPMENT FAILURE |
| Subcause | MALFUNCTION OF CONTROL/RELIEF EQUIPMENT |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | $10,000 |
| Emergency Response | $0 |
| Other Costs | $0 |
Location Map
Incident Narrative
"AT APPROXIMATELY 20:00 ON 08MAY25, SUNOCO / NUSTAR LOCAL PERSONNEL RECEIVED A CALL FROM A LANDOWNER THAT THEY SMELLED AMMONIA ANHYDROUS. LOCAL PERSONNEL DISPATCHED TO THE SITE, ARRIVING AT APPROXIMATELY 21:05 TO BEGIN WALKING THE LINE AND LOOKING FOR A LEAK. THE LEAK WAS CONFIRMED AT 21:32 WITH A CALL TO AMMONIA SYSTEM LEADERSHIP. SUNOCO / NUSTAR PIPELINE SAFETY PERSONNEL WERE NOTIFIED OF THE RELEASE AT 22:01 TO BEGIN THE NOTIFICATION PROCESS WITH THE NATIONAL RESPONSE CENTER (NRC). A CALL WAS PLACED AND RECEIVED BY THE NRC AT 22:19. MR. DAVIS TOOK THE CALL AND PROVIDED INCIDENT NUMBER 1430608. A FOLLOW-UP CALL WAS RECEIVED BY REGION 6 EPA AT 23:06 REQUESTING AN UPDATE ON THE INCIDENT AND AN OFFER TO PROVIDE ASSISTANCE, IF NEEDED. A SMALL VAPOR STREAM WAS IDENTIFIED COMING FROM THE UPSTREAM SIDE OF VALVE 3-27. CONTROL CENTER PERSONNEL WERE NOTIFIED OF THE RELEASE AND ASKED TO SHUT DOWN THE PIPELINE (22:15). LOCAL PERSONNEL WERE DISPATCHED TO CLOSE THE UPSTREAM VALVE (3-25) AND THE DOWNSTREAM VALVE (3-27). LOCAL PERSONNEL PROVIDED OVERNIGHT AIR MONITORING OF THE SITE. VISQUEEN WAS USED TO COVER THE LEAK AND KEEP THE VAPORS DOWN. THERE WAS NO DANGER TO LOCAL RESIDENTS AND NO NOTIFICATIONS WERE MADE TO LOCAL AUTHORITIES. SUNOCO / NUSTAR MAINTENANCE PERSONNEL WERE CALLED AND DISPATCHED TO THE SITE FOR REPAIRS. UPON EXCAVATION OF THE VALVE SITE, A SMALL CRACK WAS DISCOVERED ON THE SIDE SEAM WELD OF A STOPPLE TEE. REPAIRS WERE COMPLETED AND THE LINE WAS RETURNED TO SERVICE AT 18:45 ON 09MAY25."
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.