PRODUCTS (SE) PIPE LINE CORPORATION

hazardous_liquid Incident —

Incident Information

Report Date
OperatorPRODUCTS (SE) PIPE LINE CORPORATION
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates30.54901, -91.16840

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

AT APPROXIMATELY 17:00 ON AUGUST 9, 2023, THE SHIFT O&M DISCOVERED AN AREA OF ROCK/SOIL THAT WAS STAINED WITH A SMALL AMOUNT, LESS THAN A HALF-GALLON, OF DIESEL NEAR TANK 6, AREA A BOOSTER SUCTION VALVE. THE OPERATOR OBSERVED THAT DIESEL WAS LEAKING UP THE VALVE STEM AND STEM TUBE AND INTO THE METAL CONTAINMENT VAULT. THE VALVE WAS OPENED, AND TANK LEVEL LOWERED TO DECREASE THE HEAD PRESSURE ON THE VALVE. THE LEAK THROUGH THE STEM CEASED. THE TOTAL AMOUNT OF PRODUCT RELEASED INTO THE VAULT WAS CALCULATED TO BE 36.70 GALLONS. CLEANUP BEGAN IMMEDIATELY USING A VACUUM TRUCK AND CREW THAT WAS ONSITE AT BATON ROUGE TANK FARM AND WAS COMPLETED ON THE SAME DAY AS THE RELEASE. ON AUGUST 10, 2023, KINDER MORGAN MECHANICS REMOVED THE VALVE TOPWORKS. INVESTIGATION BY THE MECHANICS FOUND THE VALVE LEAKED DUE TO A WORN O-RING. THE O-RING WAS REPLACED, AND VALVE PLACED BACK IN SERVICE. 9/8/2023 - ESTIMATED COST OF $1200 ADDED TO ESTIMATED COST TO OPERATOR TO BRING TOTAL TO $2,860.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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