ENERGY TRANSFER COMPANY

hazardous_liquid Incident — — August 5, 2025

Incident Information

Incident DateAugust 5, 2025
OperatorENERGY TRANSFER COMPANY
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates34.89362, -99.03817

Cause

CauseCORROSION FAILURE
SubcauseINTERNAL CORROSION

Casualties

Fatalities0
Injuries0

Costs

Property Damage$13,000
Emergency Response$5,000
Other Costs$0

Location Map

Incident Narrative

"ON 08/05/2025 AT 11:40, A LEAK WAS DISCOVERED ON THE 12-INCH BYPASS LINE AT BRETCH STATION. THE PIPELINE TECHNICIAN SHUT-IN SECTION OF LINE UPON DISCOVERY. THE LINE WAS EXPOSED AND THE LEAK WAS COMING FROM A PINHOLE LEAK AT THE 6 O'CLOCK POSITION. THE PIPE SHOWS NO ANOMALIES OR SIGNS OF EXTERNAL CORROSION. APPROXIMATELY 0.75 BARRELS (32 GALLONS) OF CRUDE OIL WAS RELEASED. LOCAL EMPLOYEES CLEANED UP PRODUCT AND REMEDIATED IMPACTED SOIL. THE LEAK WAS REPAIRED WITH A PLIDCO MECHANICAL CLAMP AND THE LINE WAS RESTARTED AT 14:00. THE FAILED PIPE WILL BE CUTOUT AND SENT TO A THIRD-PARTY LAB FOR ANALYSIS. THE CAUSE OF THE ACCIDENT IS STILL UNDER INVESTIGATION. A SUPPLEMENTAL REPORT WILL BE SUBMITTED ONCE COMPLETE. SUPPLEMENTAL & FINAL: THE INVESTIGATION DETERMINED THAT THE FAILURE WAS DUE TO INTERNAL CORROSION. THE CAUSE OF THE INTERNAL CORROSION WAS MICROBIOLOGICALLY INDUCED CORROSION (MIC) AND UNDER-DEPOSIT CORROSION. TO PREVENT REOCCURRENCE, OPERATIONS WILL INSTALL WATER TRAP AND CORROSION COUPON AT LOWEST ACCESSIBLE LOCATION, AND DETERMINE APPROPRIATE BIOCIDE AND DOSAGE FOR TREATMENT OF THE LINE. ADDITIONALLY, EVALUATE FLUSHING VOLUME TO ENSURE TURBULENCE IS SUFFICIENT TO REMOVE DEPOSITS."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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