DENBURY GULF COAST PIPELINES, LLC
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | DENBURY GULF COAST PIPELINES, LLC |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 32.69390, -90.44080 |
Cause
| Cause | EQUIPMENT FAILURE |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
ON 10/2/2023 AT 14:00, DENBURY OPERATING PERSONNEL ARRIVED AT TINSLEY METER STATION, OBSERVED A CO2 LEAK COMING FROM A THREADED 1"" HAMMER UNION BETWEEN THE KICKER BYPASS VALVE AND RECEIVER. FIELD MANAGEMENT WAS NOTIFIED. PER DENBURY'S OM0213, THE LEAK WAS CLASSIFIED AS NON-HAZARDOUS AND SCHEDULED TO BE REPAIRED AS SOON AS PRACTICAL. THE DENBURY CONTROL CENTER DID NOT RECEIVE AN ALARM OR IDENTIFY ANY LOSS OF PRESSURE OR PRODUCT FROM THE LOCATION OF THE LEAK DUE TO THE SMALL SIZE OF THE LEAK AND IT BEING ON AN ISOLATED SECTION OF THE PIG RECEIVER PIPING. CONSIDERING THE VOLUME OF CO2 BEING RELEASED, DENBURY DETERMINED THIS LEAK TO BE NON-SIGNIFICANT, THEREFORE A NATIONAL RESPONSE CENTER (NRC) NOTIFICATION WAS NOT REQUIRED. DENBURY PERSONNEL ARRIVED ONSITE ON 10/17/2023 TO BEGIN REPAIRING THE LEAK. THE SYSTEM WAS RETURNED TO NORMAL OPERATION AFTER THE LEAK WAS REPAIRED ON 10/17/2023 AT 10:00.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.