ENERGY TRANSFER COMPANY

hazardous_liquid Incident — — September 28, 2025

Incident Information

Incident DateSeptember 28, 2025
OperatorENERGY TRANSFER COMPANY
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates32.30697, -101.89728

Cause

CauseEQUIPMENT FAILURE
SubcausePUMP OR PUMP-RELATED EQUIPMENT

Casualties

Fatalities0
Injuries0

Costs

Property Damage$4,083
Emergency Response$5,342
Other Costs$0

Location Map

Incident Narrative

"ON 09/28/2025 AT 02:46, A PIPELINE CONTROLLER RECEIVED A LOCK OUT ALARM AT RC SMITH FOR UNIT 3100 AND A PIPELINE TECHNICIAN WAS CALLED OUT TO THE STATION. THE PIPELINE CONTROLLER RECEIVED A HIGH-HIGH SUMP LEVEL ALARM AND LOCKED OUT ALL UNITS. APPROXIMATELY 15 BARREL OF CRUDE OIL WAS RELEASED. CLEANUP CONTRACTORS REMOVED PRODUCT AND REMEDIATED IMPACTED SOIL. THE CAUSE OF THE RELEASE IS STILL UNDER INVESTIGATION AND A SUPPLEMENTAL REPORT WILL BE FILED AFTER THE INVESTIGATION IS COMPLETE. SUPPLEMENTAL & FINAL: THE INVESTIGATION DETERMINED THE CAUSE OF THE ACCIDENT WAS DUE TO A PUMP-RELATED EQUIPMENT FAILURE. THE PACKING NUT LOOSENED RELEASING THE PRESSURE PACKING THAT PREVENTS OIL LEAKAGE FROM THE PLUNGER BOX. THE FAILURE OF THE PACKING ALLOWED CRUDE FLOW TO THE SUMP WHICH CAUSED AN OVERFILL. TO PREVENT RECURRENCE THE PACKING AND BRASS COMPONENTS INSIDE THE STUFFING BOX WERE REPLACED AND A BOLT WAS TAPPED AND INSTALLED ON THE PACKING NUT TO PREVENT LOOSENING DURING OPERATION."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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