COLONIAL PIPELINE CO

hazardous_liquid Incident — — December 16, 2025

Incident Information

Incident DateDecember 16, 2025
OperatorCOLONIAL PIPELINE CO
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates34.55307, -82.48787

Cause

CauseNATURAL FORCE DAMAGE
SubcauseTEMPERATURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$1,000
Emergency Response$2,167
Other Costs$0

Location Map

Incident Narrative

"ON DECEMBER 16, 2025, AT APPROXIMATELY 18:05, A LEAK WAS DISCOVERED AT THE BELTON STATION DURING A ROUTINE CHECK. THE SOURCE WAS IDENTIFIED AS THE L02 PROVER, WHERE A FAILED GASKET BETWEEN A VALVE AND BLIND FLANGE ON THE 2-INCH WATER DRAW LINE CAUSED THE RELEASE OF ULTRA-LOW SULFUR DIESEL (ULSD). THE PROVER WAS IMMEDIATELY ISOLATED. TECHNICIANS CONFIRMED THE GASKET FAILURE AS THE ROOT CAUSE. CORRECTIVE ACTIONS INCLUDED REPLACING THE GASKET AND THE 2-INCH VALVE ON THE WATER DRAW PIPING."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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