EXPLORER PIPELINE CO

hazardous_liquid Incident —

Incident Information

Report Date
OperatorEXPLORER PIPELINE CO
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates29.71731, -95.18025

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON 12.17.23 AT APPROXIMATELY 20:35 A RELEASE OF 4.1 BARRELS OF NAPTHA WAS DISCOVERED BY LOCAL OPERATIONS FROM THE INBOARD PUMP SEAL BEARING BRACKET ON UNIT 3. UPON DISCOVERY, THE LINE SEGMENT WAS SHUT DOWN AND UNIT 3 WAS ISOLATED. THE NAPTHA WAS TOTALLY CONTAINED ON THE PROPERTY AND APPROPRIATE RECOVERY AND REMEDIATION WAS CONDUCTED. THE INBOARD PUMP SEAL WAS SUBMITTED TO A THIRD-PARTY FIRM FOR A FAILURE ANALYSIS THAT INDICATED THE PRIMARY RING HAD FRETTING ON THE DRIVE NOTCHES AND THE DRIVE DENTS IN THE RETAINER WERE LIKELY SUSTAINED FROM VIBRATION AND AXIAL SHAFT MOVEMENT. THE INVESTIGATION ALSO CONFIRMED THAT THE PUMP SEAL MITIGATION SYSTEM DID WORK PROPERLY DUE TO SCALE PLUGGING THE BASIN DRAIN LINE. EXPLORER IS CURRENTLY CHANGING STEEL DRAIN LINES TO STAINLESS STEEL TUBING TO ELIMINATE SCALE AND RUST BUILDUP WITHIN ANY PUMP DRAIN SYSTEMS.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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