CCPS TRANSPORTATION, LLC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorCCPS TRANSPORTATION, LLC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates40.94090, -88.64150

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON JANUARY 3, 2024, AT 11:09 CST, THE EDMONTON CONTROL CENTER RECEIVED A GAS ALARM IN THE LINE 59 SAMPLE BUILDING AT FLANAGAN TERMINAL. AT APPROXIMATELY 11:12 CST FIELD PERSONNEL CONFIRMED A RELEASE CONTAINED WITHIN THE SAMPLE BUILDING AND LINE 59 WAS SHUT DOWN. THE SOURCE OF THE RELEASE WAS IDENTIFIED AS A CRACK IN THE CELL SAMPLER THAT SPRAYED APPROXIMATELY 20 GALLONS OF CRUDE OIL ONTO THE INTERIOR WALLS. CLEAN-UP ACTIVITIES WERE STARTED AND PERMISSION TO RESTART LINE 59 WITHOUT THE SAMPLE BUILDING WAS GIVEN TO THE CONTROL CENTER. THE SAMPLER WAS REPLACED, CLEAN-UP WAS COMPLETED, AND CLEAN-UP MATERIAL WAS PROPERLY DISPOSED. THE CAUSE OF THE RELEASE WAS IDENTIFIED AS FRACTURED HOUSING ON THE SAMPLER DUE TO FATIGUE. THE FATIGUE CRACKING HAD INITIATED AND PROPAGATED FROM SURFACE CRACKS IN THE COATING AS A RESULT OF SERVICE-RELATED STRESSES, PROGRESSIVELY REDUCING THE EFFECTIVE CROSS-SECTION OF THE HOUSING UNTIL THE LOADING EXCEEDED THE LOAD CAPACITY OF THE CRACKED HOUSING, RESULTING IN OVERLOAD FAILURE OF THE HOUSING.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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