BPX MIDSTREAM LLC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorBPX MIDSTREAM LLC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates31.87572, -103.95883

Cause

CauseNATURAL FORCE DAMAGE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

AN I&E TECHNICIAN ARRIVED ON-SITE AROUND 14:07 (CT) ON JANUARY 18, 2024, TO FIND AN ABNORMAL OPERATING CONDITION AND CONTACTED APPROPRIATE OPERATIONS PERSONNEL. LOCAL OPERATIONS PERSONNEL ARRIVED ON-SITE AT APPROXIMATELY 14:45 (CT) TO ASSESS LEAKS ON TWO OF THREE 2"" BALL VALVES ON THE BYPASS LINE. AN INITIAL RELEASE ESTIMATE INDICATED THAT LESS THAN 3 GALLONS CONTACTED THE SOIL AND WAS CONFINED TO COMPANY PROPERTY. CONTAINMENT WAS PLACED TO COLLECT THE LEAKING PRODUCT. ONCE THE IMPACTED SOIL WAS REMOVED IT WAS DETERMINED THAT 5.6 GALLONS OF PRODUCT WAS RELEASED, AND APPROPRIATE AGENCIES WERE CONTACTED ONCE THE REPORTING CRITERIA WAS MET. EXTREME COLD TEMPERATURES ARE BELIEVED TO HAVE CONTRIBUTED TO THE INITIATION OF THE LEAK. UPON DISCOVERY OF THE LEAK AND UNTIL REPAIRS COULD BE MADE, THE LEAK WAS MONITORED 24/7. REPAIRS WERE COMPLETED ON TUESDAY, JANUARY 23, 2024. THE ROOT CAUSE FAILURE ANALYSIS INDICATES THE RELEASE WAS DUE TO STAGNANT WATER.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

Back to All Incidents More Incidents in