ORYX DELAWARE OIL TRANSPORT LLC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorORYX DELAWARE OIL TRANSPORT LLC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates32.29649, -104.12380

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

APPROXIMATELY 6 BARRELS OF CRUDE OIL WERE RELEASED FROM SUMP 2090 AT ORYX CARLSBAD STATION. THE DATE AND TIME OF THE RELEASE (PART A Q4) ARE INDICATIVE OF THE EARLIEST POSSIBLE DATE/TIME THE RELEASE COULD HAVE STARTED BASED ON CONTROL CENTER INFORMATION. THE CAUSE OF THE RELEASE IS ATTRIBUTED TO EQUIPMENT FAILURE OF A CHECK VALVE LIKELY AS A RESULT OF DEBRIS CAUGHT IN THE CHECK VALVE, ALLOWING THE SUMP TO OVERFILL. ADDITIONALLY, THE SUMP HI-HI ALARM FAILED TO ALARM DUE TO PROGRAM SETTINGS THAT WERE NOT RE-SET FOLLOWING TESTING. TO PREVENT FUTURE INCIDENTS, THE CHECK VALVE WAS REPLACED AND THE PROGRAMMING ON THE SUMP HI-HI ALARM WAS RESET, TESTED, AND VERIFIED. SUPPLEMENTAL NARRATIVE (1): UPDATES APPLIED TO QUESTION 8 IN PART D.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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