ONEOK NGL PIPELINE, LLC
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | ONEOK NGL PIPELINE, LLC |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 36.58287, -98.30110 |
Cause
| Cause | INCORRECT OPERATION |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
ON MAY, 27TH 2024 PIPELINE CONTROL RECEIVED A GAS DETECT ALARM FROM HELENA BOOSTER. ONEOK PERSONNEL WERE DISPATCHED TO THE LOCATION AND DISCOVERED A TUBING LEAK ON THE PUMP 2 BEARING COOLING LINE. ONEOK PERSONNEL DETERMINED THE TUBING WAS NOT APPROPRIATELY TIGHTENED AT THE CONNECTION POINT. THE LOOSE TUBING CONNECTION WAS DETERMINED TO BE THE CAUSE OF THE RELEASE. THE LOOSE TUBING CONNECTION WAS REPAIRED.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.