TARGA DOWNSTREAM LLC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorTARGA DOWNSTREAM LLC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates31.59637, -96.10478

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

TARGA PERSONNEL RECEIVED CALL FROM TARGA'S NGL CONTROL CENTER ABOUT GAS DETECTORS INDICATING A POSSIBLE LEAK AT PUMP STATION 10. SUPERVISOR DISPATCHED PERSONNEL TO SITE TO INVESTIGATE. UPON ARRIVAL, TECHNICIAN FOUND PRODUCT ESCAPING FROM TUBING FITTINGS ON POPPET VALVE ON PUMP 140. TUBING BECAME DETACHED ALLOWING PRODUCT TO ESCAPE. TECHNICIAN SHUT IN PUMP STATION. REPAIRS WERE MADE AND STATION RETURNED TO SERVICE WITHIN APPROXIMATELY 2 HOURS. CORRECTION: REVISE PART G SUB-CAUSE FROM IMPROPER INSTALLATION TO EXCESSIVE VIBRATION. UPON FURTHER INVESTIGATION, IT WAS DETERMINED PUMP VIBRATION LOOSENED THE TUBING AND ALLOWED THE PRODUCT RELEASE. SUBSEQUENT REMEDIATION INCLUDED INSTALLATION OF CLAMPS WITH RUBBER DAMPENING TO ABSORB THE PUMP VIBRATION AND IMPLEMENTATION OF ROUTINE TUBING INSPECTION.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

Back to All Incidents More Incidents in