TRANSCONTINENTAL GAS PIPE LINE COMPANY

gas_transmission Incident — — February 18, 2025

Incident Information

Incident DateFebruary 18, 2025
OperatorTRANSCONTINENTAL GAS PIPE LINE COMPANY
CommodityNATURAL GAS
Pipeline Typegas_transmission

Location

State
Coordinates36.65607, -77.65957

Cause

CauseMATERIAL FAILURE OF PIPE OR WELD
SubcauseENVIRONMENTAL CRACKING-RELATED

Casualties

Fatalities0
Injuries0

Costs

Property Damage$222,000
Emergency Response$19,863
Other Costs$0

Location Map

Incident Narrative

"OPERATIONS DISCOVERED GAS LEAK AT MP 97.15 ON SVL-T-T-T WITH HANDHELD LEAK SURVEY EQUIPMENT. AFTER CONFIRMATION, LINE PRESSURE WAS REGULATED TO 80% OF OPERATING PRESSURE AND EXISTING PRESSURE WAS DRAWN DOWN BY A DOWNSTREAM CUSTOMER. AFTER EXCAVATION, A TRANSVERSE CRACK WAS VISUALLY IDENTIFIED ON THE PIPE BODY. THE LINE WAS SUBSEQUENTLY ISOLATED, FURTHER DRAWN DOWN BY CUSTOMERS WITH REMAINING PRESSURE BLOWN DOWN. THE PIPE SEGMENT WAS THEN CUT OUT AND REPLACED WITH PRETESTED PIPING. THE CUTOUT PIPE WAS SENT TO A METALLURGICAL LAB FOR ANALYSIS. LAB ANALYSIS CONCLUDED THE FOLLOWING: THE PRIMARY FAILURE MECHANISM WAS STRESS CORROSION CRACKING (SCC), DRIVEN BY RESIDUAL TENSILE STRESSES FROM PREEXISTING BENDING DURING CONSTRUCTION IN COMBINATION WITH A MILDLY CORROSIVE, OXYGEN-DEPLETED ENVIRONMENT. SCC MAY NOT HAVE OCCURRED IN THE ABSENCE OF PIPE BENDING DURING CONSTRUCTION, HIGHLIGHTING THE CRITICAL ROLE OF MECHANICAL LOADING IN THIS FAILURE. UNINTENTIONAL LOSS VOLUME WAS UPDATED AND REDUCED AFTER FURTHER ANALYSIS."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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