"DTM LOUISIANA GATHERING, LLC"

gas_transmission Incident — — June 16, 2025

Incident Information

Incident DateJune 16, 2025
Operator"DTM LOUISIANA GATHERING, LLC"
CommodityNATURAL GAS
Pipeline Typegas_transmission

Location

State
Coordinates32.06810, -93.90910

Cause

CauseCORROSION FAILURE
SubcauseINTERNAL CORROSION

Casualties

Fatalities0
Injuries0

Costs

Property Damage$190,000
Emergency Response$0
Other Costs$0

Location Map

Incident Narrative

"ON JUNE 16, 2025, AT APPROXIMATELY 0815 HOURS, A RUPTURE OCCURRED IN A BORED SECTION OF THE PIPELINE. THIS RESULTED IN AN UNINTENTIONAL RELEASE OF NATURAL GAS EXCEEDING 3 MMCF. DTM'S FIELD TECHNICIANS RESPONDED TO THE UNINTENTIONAL RELEASE, ISOLATING THE AFFECTED SECTION OF THE PIPELINE AND PREVENTING FURTHER RELEASE. THE CAUSE OF THE FAILURE IS STILL UNDER INVESTIGATION. THE FAILED SECTION OF PIPE HAS BEEN REMOVED AND SENT OFF FOR A COMPLETE ANALYSIS. A SUPPLEMENTAL REPORT WILL BE SUBMITTED WHEN DTM HAS MORE INFORMATION. THIS REPORT PROVIDES THE FINAL RESPONSE AND CLOSURE TO THE ORIGINAL FILING SUBMITTED ON JUNE 16, 2025, FOLLOWING COMPLETION OF THE SUBSEQUENT ASSESSMENT. DT MIDSTREAM HAS REACHED A FINAL DETERMINATION TO REPLACE THE ENTIRE 3,546-FOOT SECTION OF PIPELINE. THIS DECISION WAS MADE IN CONSIDERATION OF THE POTENTIAL FOR ADDITIONAL AREAS OF CONCERN IDENTIFIED WITHIN OTHER LOW-LYING PORTIONS OF THE PIPELINE SEGMENT. SUPPLEMENT: UPON REVIEWING THIS RELEASE WITH THE STATE OF LOUISIANA, I IDENTIFIED A TYPOGRAPHICAL ERROR IN THE INITIAL TIMES REPORTED FOR ON SCENE AND CONFIRMED DISCOVERY. THE TIMES HAVE BEEN UPDATED TO REFLECT ACCURACY."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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