STAGECOACH GAS SERVICES LLC
gas_transmission Incident — — October 8, 2025
Incident Information
| Incident Date | October 8, 2025 |
| Operator | STAGECOACH GAS SERVICES LLC |
| Commodity | NATURAL GAS |
| Pipeline Type | gas_transmission |
Location
| State | |
| Coordinates | 42.41595, -76.89717 |
Cause
| Cause | EQUIPMENT FAILURE |
| Subcause | MALFUNCTION OF CONTROL/RELIEF EQUIPMENT |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | $0 |
| Emergency Response | $100 |
| Other Costs | $0 |
Location Map
Incident Narrative
"ON OCTOBER 8TH, 2025, A RELIEF VALVE AT THE SENECA LAKE STORAGE FACILITY ACTIVATED AND VENTED 20,730 MCF OF NATURAL GAS INTO THE ATMOSPHERE. A KINDER MORGAN EMPLOYEE ARRIVED AT THE LOCATION AND CONFIRMED THE RELEASE. THE MAOP WAS NOT EXCEEDED AND THE GAS VENTING LASTED FOR APPROXIMATELY 3HRS AND 7 MINUTES. AN INTERNAL INVESTIGATION IS CURRENTLY ONGOING, AND A FINAL REPORT WILL BE SUBMITTED ONCE THE INVESTIGATION DETAILS ARE FINALIZED."
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.