ENERGY TRANSFER COMPANY

gas_transmission Incident — — October 22, 2025

Incident Information

Incident DateOctober 22, 2025
OperatorENERGY TRANSFER COMPANY
CommodityNATURAL GAS
Pipeline Typegas_transmission

Location

State
Coordinates31.75988, -102.25927

Cause

CauseOTHER INCIDENT CAUSE
SubcauseUNKNOWN

Casualties

Fatalities0
Injuries0

Costs

Property Damage$880,026
Emergency Response$0
Other Costs$0

Location Map

Incident Narrative

"ON OCTOBER 22, 2025, AT 6:30 A.M. WHILE INVESTIGATING LINE SHUT-INS AND COMPRESSOR SHUTDOWNS DUE TO HIGH O2 ISSUES AN OPERATIONS (OPS) TECH OBSERVED THAT THE HEADLEE DISCHARGE LINE HAD 40 PSIG WHEN THE NORMAL OPERATING PRESSURE IS 1250 PISIG. THE EMPLOYEE NOTIFIED THE OPS SUPERVISOR WHO THEN VERIFIED THE LINE PRESSURE WITH ANOTHER OPS TECH LOCATED AT THE LUPIN STATION. AT 6:40 A.M. THE OPS TEAM BEGAN A LEAK INVESTIGATION ON THE 7406642 - LUPIN TO HEADLEE. AT 09:37 A.M. FIELD PERSONNEL PINPOINT THE LOCATION THE LEAK. THE LINE WAS SHUT IN AND FIELD PERSONNEL BEGAN TO INVESTIGATE THE SEVERITY OF THE LEAK. AT 11:15 A.M. OPERATIONS MADE AN INITIAL DETERMINATION THAT THE LEAK MAY EXCEED THE REPORTABLE THRESHOLD AND NOTIFIED DOT COMPLIANCE. THE NRC NOTIFICATION WAS MADE AT 12:06 P.M. TXRRC NOTIFICATION WAS MADE AT 12:15 P.M. THE INVESTIGATION IS ONGOING."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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