"TEXAS EASTERN TRANSMISSION, LP"

gas_transmission Incident — — November 6, 2025

Incident Information

Incident DateNovember 6, 2025
Operator"TEXAS EASTERN TRANSMISSION, LP"
CommodityNATURAL GAS
Pipeline Typegas_transmission

Location

State
Coordinates29.62031, -88.88696

Cause

CauseEQUIPMENT FAILURE
SubcauseTHREADED CONNECTION/COUPLING FAILURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$0
Emergency Response$75,000
Other Costs$13,000

Location Map

Incident Narrative

"DURING THE PURGING OPERATION OF A 16-INCH OFFSHORE PIPELINE (40-B-03) SCHEDULED FOR ABANDONMENT, A 2-INCH TEMPORARY HOSE USED FOR GAS VENTING BECAME DISCONNECTED FROM THE 16-INCH LINE APPROXIMATELY TWO HOURS INTO THE CONTROLLED PURGE. THIS DISCONNECTION RESULTED IN UNCONTROLLED UNDERWATER VENTING FOR AN ESTIMATED FIVE ADDITIONAL HOURS. THE VALVE AND TEMPORARY HOSE ASSEMBLY WERE SENT TO A LABORATORY FOR DETAILED FAILURE ANALYSIS. THE ANALYSIS DETERMINED THAT THE 2-INCH NIPPLE EXPERIENCED AN AXIAL LOAD COMBINED WITH BENDING FORCES. THESE FORCES CAUSED OVALIZATION OF THE NIPPLE CONNECTION AND ULTIMATELY LED TO SHEARING OF THE THREADED CONNECTION. THE PIPELINE (40-B-03) HAD SHUT DOWN AND ISOLATED SINCE OCTOBER."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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