ANR PIPELINE CO
gas_transmission Incident — — November 14, 2025
Incident Information
| Incident Date | November 14, 2025 |
| Operator | ANR PIPELINE CO |
| Commodity | NATURAL GAS |
| Pipeline Type | gas_transmission |
Location
| State | |
| Coordinates | 43.65406, -88.05258 |
Cause
| Cause | EXCAVATION DAMAGE |
| Subcause | EXCAVATION DAMAGE BY THIRD PARTY |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | $550,645 |
| Emergency Response | $0 |
| Other Costs | $0 |
Location Map
Incident Narrative
"NOTIFICATION FROM THE PUBLIC WAS RECEIVED OF A POSSIBLE THIRD-PARTY LINE STRIKE ON NOVEMBER 14, 2025, FIRST RESPONDERS ONSITE CONFIRMED BLOWING GAS ON THE ANR 1-380 PIPELINE AT 14:05 CST. ANR PIPELINE'S GAS CONTROL VERIFIED THE PRESSURE DROP AT 14:10 CST. UPON ARRIVAL AT THE SITE, THE TECHNICIAN CONFIRMED THE GAS RELEASE WAS CAUSED BY A THIRD-PARTY CONTRACTOR'S EQUIPMENT. IMMEDIATE ACTIONS WERE TAKEN TO ISOLATE THE PIPELINE BY CLOSING THE UPSTREAM AND DOWNSTREAM VALVES. THERE WERE 4 ASSOCIATED INJURIES THAT WERE TREATED AND RELEASED, NO OVERNIGHT HOSPITALIZATIONS AND NO IGNITION OCCURRED. EXCAVATION APPEARS TO BE OUTSIDE THE ONE-CALL TICKET WORK ZONE, INVESTIGATION IS ONGOING. GAS WAS RESTORED ON ANR 1-380 PIPELINE AND RETURNED TO SERVICE NOVEMBER 17, 2025, AT 18:22 CST. ESTIMATED COST OF PUBLIC AND NON-OPERATOR PRIVATE PROPERTY IS STILL BEING EVALUATED. REPAIR COSTS ARE ESTIMATES AND WILL BE UPDATED WITH THE FORTHCOMING SUPPLEMENTAL REPORT."
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.