DAKOTA GASIFICATION COMPANY

gas_transmission Incident — — December 10, 2025

Incident Information

Incident DateDecember 10, 2025
OperatorDAKOTA GASIFICATION COMPANY
CommodityNATURAL GAS
Pipeline Typegas_transmission

Location

State
Coordinates47.37546, -101.83826

Cause

CauseEQUIPMENT FAILURE
SubcauseMALFUNCTION OF CONTROL/RELIEF EQUIPMENT

Casualties

Fatalities0
Injuries0

Costs

Property Damage$0
Emergency Response$500
Other Costs$0

Location Map

Incident Narrative

"AT 0450 ON 12/10/2025 A REMOTE-CONTROLLED BLOCK VALVE ON A VENT STACK AT A METERING STATION OPENED DUE TO AN APPARENT FAILURE OF THE POWER GAS SUPPLYING A PNEUMATIC ACTUATOR. IT IS BELIEVED THAT MOISTURE IN THE POWER GAS SUPPLY SYSTEM FROZE UP THE TUBING OR REGULATORS AFTER THE HEAT TRACING AROUND THE ACTUATOR FAILED. THE ACTUATOR IS DESIGNED TO OPEN THE VALVE DURING FAILURE AS PART OF THE EMERGENCY SHUTDOWN SYSTEM AT THE STATION. AT 0544 THE CONTROL ROOM OPERATOR CLOSED THE REMOTE-CONTROLLED BLOCK VALVE UPSTREAM OF THE VENT STACK TO STOP THE RELEASE. AT APPROXIMATELY 0600 PIPELINE OPERATIONS PERSONNEL ARRIVED AT THE STATION AND CLOSED A MANUAL BLOCK VALVE ON THE VENT STACK. TO DETERMINE THE EXTENT OF THE RELEASE, AN INITIAL REVIEW OF THE PROCESS CONDITIONS WAS COMPLETED AT 1138 WHICH INDICATED THE RELEASE WAS LIKELY GREATER THAN 3 MMCF. SUBSEQUENT HYDRAULIC CALCULATIONS DETERMINED 6.38 MMCF OF NATURAL GAS WAS RELEASED. THE RELEASED GAS DID NOT IGNITE AND THERE WERE NO INJURIES OR EVACUATIONS."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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